Today was an initially frustrating and then rewarding day of work on Lorene. It almost seemed like Christmas when I got home from work -- my LED bulb, belt, bed cushions and drip pad all arrived! I didn’t get started until later in the evening because of physical therapy, dinner and an errand. I started by chiseling out the remaining bits of the bed cushions. I wonder what those things were made out of, because they really looked like they had melted. Once I got the bits out, I put on the new cushions. Then I removed the drip pan to do some more cleaning of the grease. After that, I oiled and lubricated. I turned the main shaft (the hand wheel was off) and oiled wherever I saw parts moving against each other. I put the new drip pad onto the pan, found new felt circles, and closed up the underside of the machine. I ended up having to remove the drip pan later, but that’s another part of today’s story.
I moved on to oiling the upper part of the machine. I moved the spool pin plate and lubricated the gears. I put oil wherever it looked necessary. After closing that up, I oiled anywhere I could remember from my workshop last May. I oiled all the moving parts that I could see in the needle-bar and presser-foot assemblies (behind the face plate). I removed more lint that was in there, too. I was happily moving the main shaft and listening and oiling, and getting so excited about getting close to finishing so I could actually try to sew.
And then…
I realized something. Sure, the hook assembly was moving just fine, but the bobbin case base was moving along with it. The little “finger” that sticks up and fits into the slot on the needle plate was moving with the hook. I had oiled behind the base so I thought it would move with a little elbow grease. Wrong. I couldn’t get it to move, and Bill couldn’t get it to move. Fine, I thought. I’ll go ahead and remove the hook assembly like I saw in an April 1930s video last week. Someone obviously already tried that, because the screws are pretty well stripped.
I was starting to think I’d never get this machine working again. I couldn’t get to the hook so I could remove whatever thread was hiding behind the bobbin case base. I was trying and trying to make the base move, to no avail. Finally, Bill mentioned WD-40. A-ha! I had read somewhere that it could dissolve little bits of thread that were jamming the machine. I started spraying WD-40 onto the hook assembly. Jiggle the base. More WD-40. Jiggle the base. Swear at the machine. Try to get Bill to make the case move.
Bill told me to give up for the night, that it was like trying to write the last chapter of a book. It’s hard to leave it for a while, but sometimes that’s the best thing to do. I knew he was right, and that a night of soaking in WD-40 was probably a good idea.
Well, sometimes I don't listen to myself.
I couldn’t let it go without one last try, and around 10 p.m., suddenly the bobbin case base moved. It wasn’t moving smoothly, but it was moving! I kept turning the main shaft and eventually, it started to move freely! Success!
I don’t know what was holding the parts together, but it was certainly strong!
It was a satisfying project, to see how frozen and neglected this machine was, and to make it functional again.
Here’s what was on the docket for the next day:
- Take apart the tension assembly, clean, and reassemble.
- Clean the stop-motion washer and faceplate.
- Put a seam-allowance sticker from Sew Classic onto the needle plate.
- Install the belt.
- Put in the new light bulb.
- Clean and maybe wax.
I didn’t know if all of that would be accomplished the next day, but I hoped to be able to try to sew with Lenore the day after that.
I wondered what I would do when this project was over. Actually sew something?



